1887

Abstract

Summary

This paper covers actual instances of how the service reduced potential NPT/ILT through identified and mitigated issues related to real time hole cleaning, drilling and hydraulics optimization, correct hole volume for cementing, and in some extend the effectiveness and efficiency of viscous pill for stuck pipe avoidance in horizontal and extended reach wells.

Loading

Article metrics loading...

/content/papers/10.3997/2214-4609.201901904
2019-05-27
2020-11-24
Loading full text...

Full text loading...

References

  1. Fabrizio, Z., Vallorani, F., Concas, A., Cavallaro, G., Giorgio, M., Cesaro, M., Bezzola, C., Angleraux, F., Kerherve, J.
    , “How to Improve Drilling Efficiency Using the Cutting WeightingTechnology” Paper presented in the Offshore Mediterranean Conference – OMC2005.
    [Google Scholar]
  2. Zausa, F., Civolani, L., Brignoli, M., Santarelli, F.J.
    , “Real-Time Wellbore Stability Analysis at the Rig Site” Paper SPE/IADC 37670, presented at the 1997 SPE/IADC Drilling Conference held in Amsterdam, The Netherlands, 4-6 March 1997.
    [Google Scholar]
  3. Yuejin, L., Bern, P.A., Chambers, B.D.
    , “Simple Charts to Determine Hole Cleaning Requirementsin Deviated wells” Paper IADC/SPE 27486, presented at the 1994 IADC/SPE Drilling Conference in Dallas, Texas, 15-18 February 1994.
    [Google Scholar]
http://instance.metastore.ingenta.com/content/papers/10.3997/2214-4609.201901904
Loading
/content/papers/10.3997/2214-4609.201901904
Loading

Data & Media loading...

This is a required field
Please enter a valid email address
Approval was a Success
Invalid data
An Error Occurred
Approval was partially successful, following selected items could not be processed due to error