1887

Abstract

For years Saudi Aramco faced rapid and chronic Claus catalyst deactivation induced by aromatics (BTX) in feed acid gas (lean<br>acid gas). This catalyst deactivation resulted in low sulfur recovery and frequent shutdowns to replace the catalyst. After<br>completing an exhaustive process selection study to identify the most cost effective solution to the problem, the company<br>proceeded with installation of regenerable activated carbon beds upstream of sulfur recovery units (SRUs) to remove<br>aromatics contaminants before they reach the converter beds.

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/content/papers/10.3997/2214-4609-pdb.148.iptc12123
2008-12-03
2024-04-28
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http://instance.metastore.ingenta.com/content/papers/10.3997/2214-4609-pdb.148.iptc12123
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